Installation of the packer's and the 40 mm lift springs was a straightforward task. I had the advantage of two overhead gantry cranes that my
disposal, and a willing friend to help. With one crane attached to the front of the vehicle, and one attached to the rear, all four packers and springs were fitted in 1.5 hours.A quick check with the tape
measure indicated that true to design, 100 mm of lift had been achieved.
The visual transformation was impressive. The icon of British aristocracy had just obtained "ATTITUDE"!!
The suspected
consequences of such a radical lift were now physically apparent, and my original theories could be tested. The checklist was ticked off and the remaining tasks prioritised.
Firstly, new longer brake lines were
required. I decided to go for longevity, and fitted stainless steel braided Teflon hoses. I had to supply the hydraulic experts with an original brake hose so that they could identify the end fittings.
They supplied me with re-usable hose ends, and a roll of braided hose. I simply had to cut the hose to length and attach the fittings.
Stainless braided brake lines (plastic tubing to protect the braid.)
The second item on the checklist was the rear shock absorber top mountings. These needed to be lowered by 100mm in order to maintain the original working stroke of the shock absorber. It wasn't
practical to reuse the original mount, but I wanted to reuse the original mounting holes in the chassis. I fabricated new mounting plates from 10mm steel, and drilled the mounting holes as per
the original shock mounts. I enlisted the help of a local engineering firm, and they machined two new mounting pins, machined to the correct angle, which I welded to the mounting plates.
Unfortunately, due to the location of the bottom mounting hole, I could only lower the shock mount 75 mm.
Rear top shock mount, bolted via original mounting holes.
As a cautionary note, when welding suspension parts, ensure that low hydrogen rods are used, and
always preheat to 150-200 deg C. This will minimise hydrogen imbrittlement, and possible weld failure.
The next modification, which was more critical to the vehicles on road handling than it's off road
performance, was the re-setting of the front swing arms. If left unmodified, the "straight" swing arm was placing excessive strain on the rubber bushing at the chassis mounting, and produced major
bump steer at highway speeds due to the incorrect kingpin angle.
To complete this task I drafted a full sized layout of the original swing arm, and over laid the required
new position after the 100mm lift. This enabled me to mark the swing arms with the locations of the bends and their appropriate angles.
As a tip, if you undertake to bend your swing arms, make sure you have a very large heating rose, and at least 2m of suitably sized galv pipe to complete the task. Even when heated bright red, the
arms were still very difficult to bend.
Once re fitted to the vehicle, a visual improvement could be seen in the inclination of the front axle, and the chassis mounting bushes were no longer stressed.
However, the first unforeseen consequence of the lift soon became apparent. During the first test drive a rather unhealthy noise was being transmitted through the drive train on de-acceleration. A
closer inspection revealed that the front drive shaft universal on the diff end was exceeding its maximum working angle. The yoke castings were actually bottoming out on each other, and this
was on level ground. Under cross up conditions, the universal would have exploded!
I made the decision to fit a CV joint to the drive shaft. Fitting a CV joint had several other
advantages. First, the CV joint is longer than a standard universal knuckle which generated a greater clearance between the drive shaft and the chassis cross member in front of the gearbox.
Secondly, because I was modifying the drive shaft anyway, it enabled me to have the drive shaft made 15 mm longer than standard and maintain the original length of spline engagement.
The drive shaft was modified and refitted to the vehicle, but during the test runs I could not solve a high-speed vibration in the driveline. After consulting some overseas experts via e-mail it became
apparent that when a CV joint is fitted to a drive shaft, the universal angle into the diff head must be straight. Due to the resetting of the swing arms my universal angle was approximately 10 degrees.
So, out came the swing arms, the heating rose, the length of pipe, and my patient assistant. After re-re-setting the swing arm angles, all but the smallest of vibrations were removed.
Certification
The next major task to be completed was to pass the dreaded vehicle inspection and certification. I took the vehicle to Quality Automotive in East Tamaki who were at the time, certified vehicle
inspectors. The difficulty is that once you have modified one small item on a vehicle, the entire vehicle requires re-certification.
The engineers had the vehicle for a full day and were very thorough with their inspection. They failed the vehicle on three counts:
- 2 of the gearbox mounting bolts were not secured with spring washes.
- as a precautionary measure the rear drive shaft required a drive shaft catcher to contain the drive shaft should it snap or break a universal joint.
- the engineers were not happy with, nor could they find a ruling regarding the heating and bending of suspension swing arms.
Fixing the first two issues were easy. Two new spring washes and a drive shaft catcher bolted through the floor pan were quickly install. However, the modified swing arms seemed to have all the
expects scratching the heads. Numerous phone calls to Wellington concluded that if I could supply a materials testing report, complete with the signature of a suitably qualified person, which stated
that the structural strength of the swing arms had not been severely affected, they would allow them to pass.
I phoned Heated Treatments Limited and spoke to their Quality Engineer. He was more than happy
to carry out some comparison hardness testing between the heated and unheated areas on the swing arms. This was duly completed, and revealed that the original steel hardness was
approximately 17 Rockwell C, and the heat affected steel was approximately 15 Rockwell C. (For any other you who have an understanding of steel hardness, the swing arms are manufactured from
very soft steel. They have probably been designed this way so that they act as a crumple zone in the event of an accident)
The Quality Engineer was more than happy with the results and supplied me with a certificate to that effect. This in turn satisfied the Certifying Engineers.
Part 3
The key to off road performance of any vehicle is "balance". All things have to work in harmony
with one another. This includes everything from the driver input to the tyres that touch the ground.
The function of the suspension system is to keep the tyres on the ground at all times. If the tyres
lose contact, traction is lost, and you lose forward momentum. This may seem all too obvious, and I am not trying to tell anyone how to suck eggs, but this is all too often overlooked when carrying
out suspension modifications.
As with any modification, the proof is always in the pudding. Up until the first off road excursion, I
had no idea as to whether or not all the calculations and hard work was going to pay off. There was always the fear that I may have weakened the integrity of the original set up. I had to rebuild my
confidence, and overcome my fear of breaking something.
My confidence grew after each consecutive off road excursion. A number of these were conducted
in the Rotorua and Taupo areas, and I cringed at the thought of having to be towed home from so far afield. But to date, no part of the suspension modification has failed or caused me any real
concern. (Except for the CV joint fitted to the front drive shaft. Due to some over zealous greasing I managed to push out one of the grease seals which bound up the joint)
The Range Rover's performance off road has been outstanding. At this stage I have no more axle articulation than a standard spec'd vehicle, but I do here 100mm of extra ground clearance, which is
a big help considering that the Range Rover suffers from a long rear overhang. The combination of the 40mm lift King springs and the standard length Koni shocks work extremely well. I think the
slightly softer spring rate over the 50mm springs is an asset. To date I have only ever bottomed out the suspension system two or three times, and that was always at a very high speed and my own
silly fault. The Koni shocks are superb, and if you can afford them, they can't really be beaten for performance. Getting the shock absorber dampening correct is just as important as the right spring rate.
I have also fitted "polly air springs" to the back to help when carrying heavy loads, and I also run these pumped up to about 20psi when driving on road to help stiffen the rear springs and reduce the body roll.
Full view of the rear spring with packer and "Poly Air Spring" fitted.