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HighRange'86 EFI Range Rover

Range Rover 100mm Suspension Lift

Disclaimer

Although I am a Fitter and Turner by trade, and am certified in Power and Plant Engineering, I am the first admit that I'm not a suspension expert.  This article is intended to be a summary of the research I have conducted, and the modifications that I have carried out on my own Range Rover.  I have done my best to ensure that everything stated in this article is factually correct, but can offer no guarantees.  I highly recommend that, before undertaking any suspension modifications, you gain a full and complete understanding of the LTSA rules and regulations.  The modifications carried out on my own Range Rover were done myself and have been fully certified.  However, the rules and regulations may well have changed.  Please exercise caution.

Part 1

Background

The motivation for suspension modification usually comes from one of the following backgrounds:

    1. A desire for greater ground clearance.

    2. A desire for greater wheel arch clearance for the fitting of larger tyres.

    3. A desire for greater axe articulation.

For me, the motivation was a combination of all of the above.

My own range Rover, a 1986 EFI Vogue, was in standard road going trim when I purchased it.  It was fitted with a front spoiler, aluminium bull bar (good for mounting spotlights only), after market alloy wheels, and a rear mounted nudge bar.  I doubt very much that it had ever seen a bog hole or steep hill climb.

The event that forced my hand, and started me on the road of suspension modification, was when I purchased a set of Hankook RT01 MT 31"x10.5" tyres, mounted on a set of white spoke rims.  The combination of larger, wider tyres, mounted on rims with a greater offset, and a set of rear suspension springs that had already with stood 130,000 miles of punishment, resulted in my new tyres being dealt to buy the razor sharp edges of the wheel arch surrounds.

The easiest solution to this dilemma would have been to follow the same path that so many Range Rover owners take.  Simply fit a set of 50mm lift springs.  However, I felt in the long run, that this would be a compromise (but certainly a cheaper solution than the one I took).

The Range Rover design engineers have millions of dollars to spend on research and development, along with the necessary equipment to design, build, and test their design modifications.  If a suspension left was as simple as adding a 50 mm lift spring, why wasn't it a factory option?

Let the Design Begin

At first glance, fitting a 50 mm lift spring looks harmless enough.  However, several problems exist.

  1. The 50 mm lift spring has a higher spring rate than a standard spring.  During hard out offroading, or when carrying heavy loads, this can be a bonus.  However, the increase in the suspension stiffness can reduce axle articulation.
  2. The 50 mm lift spring is manufactured from a spring wire of approximately 2mm larger in diameter than a standard spring.  If you compare the lengths of a fully compressed standard spring with that of a 50 mm lift spring, he will find that the 50 mm lift spring is approximately 20 mm longer.  In practice, this will result in 20 mm less upward axle articulation.
  3. If left unmodified, the shock absorbers are no longer sitting at mid-stroke when the vehicle is at rest on level ground.  They are extended by an extra 50 mm.  This will mean that, when fully crossed up, the axle dropout will be reduced. 

Remembering that the fully compressed spring height of a 50 mm lift spring is also 20 mm longer than standard (as detailed above), again when fully crossed up, the spring will bottom out while the shock absorber still has approximately 20 mm of travel left.  This is wasteful.

The solution to the above problems lies with the lengths of the shock absorbers.  If you are happy with the heavier spring rate of the 50 mm lift springs, then you need new shock absorbers with a 20 mm longer compressed length, and a 50 mm longer extended length.  The closest compromise I have been able to find are the Old Man Emu shocks designed for the Nissan Patrol long wheelbase.  However, new shock absorber mounts will need to be manufactured, as the end fixtures are not the same as those for the Range Rover.

As you are beginning to see, by making one small modification, a whole host of complications exist.

Personally, I wanted more then 50 mm of lift.  Because of the 100 inch wheel base, and a long overhang, the Range Rover suffers when negotiating steep break-overs and deep trenches.  The door sills and the rear quarter body work usually takes a beating.  I wanted to get more clear air between the bodywork and the hard stuff.

Reading the American magazines and assorted web sites revealed that they were doing lifts of as much as 150 mm.  Modifications to these extents are usually extremely expensive.  Not wanting to over do it, I said my goal at a 100 mm lift.

In Search of a 100mm Lift

In Light of the above issues I set myself the following guidelines:

  1. Obtain a lift not exceeding 100 mm.
  2. Retain the softer spring rate of the original specification springs.
  3. As a minimum, maintain the original axle articulation dimensions by fitting extra length shock absorbers, or by utilising the original shock absorbers with redesigned mounting locations.
  4. Try to keep the conversion as simple as possible.  Where possible, the lift should be able to be removed at a later date to restore the vehicle to its original specifications.

Many hours were spent lying underneath the Rover trying to decide the easiest and most economic method of achieving my guidelines.  The conclusions I came to where as follows:

  1. Fit new 40mm lift King springs with a fabricated 60mm packer. The 40mm lift springs are manufactured from the same diameter spring wire is to the original Range Rover fitment, hence maintaining the same fully compressed spring height.
  2. The 60mm packer for the front spring would be fabricated such that the shock absorber mounting, and stroking, would remain as per the original.  This is possible because the front shock absorber is mounted inside the spring.  Hence, when the packer lifts the spring, it also lifts the shock absorber.
  3. New upper shock absorber mounts would be required in the rear, mounted 100 mm lower than the original.
  4. New, longer brake lines would be required due to be increased distance between the chassis and the axles.
  5. Because the 100 mm of lift would drastically change the king pin angle in the front axle, the front radius arms would require resetting.  If the kingpin angle is not restored to the original specification, the vehicles on road derivability would be seriously affected.

Part 2

In summary of part 1, I had decided on a 100 mm suspension lift, achieved by fitting 40 mm lift King springs, 60mm spring packers, repositioning the rear top shock mounts, and resetting the front swing arms.

Let the Modifications Began

The first task was to fabricate and install the packers.  The packers were to fit on top of the axle and support the spring mounting plate.  I fabricated a box type structure using 6 mm and 10 mm steel.  Mounting holes were drilled into each packer to match the original mounting holes used to secure the spring location plate.  This enabled the packer to be bolted to the axle, and the spring location plate to be bolted to the packer.  The front packers were also drilled to accommodate the mounting stem of the front shock absorber.

Due to the shock absorber having to be mounted in the center of the front spring packer, no internal bracing could be fitted.  Hence the wide foot plate and the external lateral braces.

The rear packer, complete with internal bracing.

Installation of the packer's and the 40 mm lift springs was a straightforward task.  I had the advantage of two overhead gantry cranes that my disposal, and a willing friend to help.  With one crane attached to the front of the vehicle, and one attached to the rear, all four packers and springs were fitted in 1.5 hours.

A quick check with the tape measure indicated that true to design, 100 mm of lift had been achieved.

The visual transformation was impressive.  The icon of British aristocracy had just obtained "ATTITUDE"!!

The suspected consequences of such a radical lift were now physically apparent, and my original theories could be tested.  The checklist was ticked off and the remaining tasks prioritised.

Firstly, new longer brake lines were required.  I decided to go for longevity, and fitted stainless steel braided Teflon hoses.  I had to supply the hydraulic experts with an original brake hose so that they could identify the end fittings.  They supplied me with re-usable hose ends, and a roll of braided hose.  I simply had to cut the hose to length and attach the fittings.

Stainless braided brake lines (plastic tubing to protect the braid.)

The second item on the checklist was the rear shock absorber top mountings.  These needed to be lowered by 100mm in order to maintain the original working stroke of the shock absorber.  It wasn't practical to reuse the original mount, but I wanted to reuse the original mounting holes in the chassis.  I fabricated new mounting plates from 10mm steel, and drilled the mounting holes as per the original shock mounts.  I enlisted the help of a local engineering firm, and they machined two new mounting pins, machined to the correct angle, which I welded to the mounting plates.  Unfortunately, due to the location of the bottom mounting hole, I could only lower the shock mount 75 mm.

Rear top shock mount, bolted via original mounting holes.

As a cautionary note, when welding suspension parts, ensure that low hydrogen rods are used, and always preheat to 150-200 deg C.  This will minimise hydrogen imbrittlement, and possible weld failure.

The next modification, which was more critical to the vehicles on road handling than it's off road performance, was the re-setting of the front swing arms.  If left unmodified, the "straight" swing arm was placing excessive strain on the rubber bushing at the chassis mounting, and produced major bump steer at highway speeds due to the incorrect kingpin angle.

To complete this task I drafted a full sized layout of the original swing arm, and over laid the required new position after the 100mm lift.  This enabled me to mark the swing arms with the locations of the bends and their appropriate angles.

As a tip, if you undertake to bend your swing arms, make sure you have a very large heating rose, and at least 2m of suitably sized galv pipe to complete the task.  Even when heated bright red, the arms were still very difficult to bend.

Once re fitted to the vehicle, a visual improvement could be seen in the inclination of the front axle, and the chassis mounting bushes were no longer stressed.

However, the first unforeseen consequence of the lift soon became apparent.  During the first test drive a rather unhealthy noise was being transmitted through the drive train on de-acceleration.  A closer inspection revealed that the front drive shaft universal on the diff end was exceeding its maximum working angle.  The yoke castings were actually bottoming out on each other, and this was on level ground.  Under cross up conditions, the universal would have exploded!

I made the decision to fit a CV joint to the drive shaft.  Fitting a CV joint had several other advantages.  First, the CV joint is longer than a standard universal knuckle which generated a greater clearance between the drive shaft and the chassis cross member in front of the gearbox.  Secondly, because I was modifying the drive shaft anyway, it enabled me to have the drive shaft made 15 mm longer than standard and maintain the original length of spline engagement.

The drive shaft was modified and refitted to the vehicle, but during the test runs I could not solve a high-speed vibration in the driveline.  After consulting some overseas experts via e-mail it became apparent that when a CV joint is fitted to a drive shaft, the universal angle into the diff head must be straight.  Due to the resetting of the swing arms my universal angle was approximately 10 degrees.  So, out came the swing arms, the heating rose, the length of pipe, and my patient assistant.  After re-re-setting the swing arm angles, all but the smallest of vibrations were removed. 

Certification

The next major task to be completed was to pass the dreaded vehicle inspection and certification.  I took the vehicle to Quality Automotive in East Tamaki who were at the time, certified vehicle inspectors.  The difficulty is that once you have modified one small item on a vehicle, the entire vehicle requires re-certification.

The engineers had the vehicle for a full day and were very thorough with their inspection.  They failed the vehicle on three counts:

  1. 2 of the gearbox mounting bolts were not secured with spring washes.
  2. as a precautionary measure the rear drive shaft required a drive shaft catcher to contain the drive shaft should it snap or break a universal joint.
  3. the engineers were not happy with, nor could they find a ruling regarding the heating and bending of suspension swing arms.

Fixing the first two issues were easy.  Two new spring washes and a drive shaft catcher bolted through the floor pan were quickly install.  However, the modified swing arms seemed to have all the expects scratching the heads.  Numerous phone calls to Wellington concluded that if I could supply a materials testing report, complete with the signature of a suitably qualified person, which stated that the structural strength of the swing arms had not been severely affected, they would allow them to pass.

I phoned Heated Treatments Limited and spoke to their Quality Engineer.  He was more than happy to carry out some comparison hardness testing between the heated and unheated areas on the swing arms.  This was duly completed, and revealed that the original steel hardness was approximately 17 Rockwell C, and the heat affected steel was approximately 15 Rockwell C.  (For any other you who have an understanding of steel hardness, the swing arms are manufactured from very soft steel.  They have probably been designed this way so that they act as a crumple zone in the event of an accident)

The Quality Engineer was more than happy with the results and supplied me with a certificate to that effect.  This in turn satisfied the Certifying Engineers.

Part 3

The key to off road performance of any vehicle is "balance".  All things have to work in harmony with one another.  This includes everything from the driver input to the tyres that touch the ground.

The function of the suspension system is to keep the tyres on the ground at all times.  If the tyres lose contact, traction is lost, and you lose forward momentum.  This may seem all too obvious, and I am not trying to tell anyone how to suck eggs, but this is all too often overlooked when carrying out suspension modifications.

As with any modification, the proof is always in the pudding.  Up until the first off road excursion, I had no idea as to whether or not all the calculations and hard work was going to pay off.  There was always the fear that I may have weakened the integrity of the original set up.  I had to rebuild my confidence, and overcome my fear of breaking something.

My confidence grew after each consecutive off road excursion.  A number of these were conducted in the Rotorua and Taupo areas, and I cringed at the thought of having to be towed home from so far afield.  But to date, no part of the suspension modification has failed or caused me any real concern.  (Except for the CV joint fitted to the front drive shaft.  Due to some over zealous greasing I managed to push out one of the grease seals which bound up the joint)

The Range Rover's performance off road has been outstanding.  At this stage I have no more axle articulation than a standard spec'd vehicle, but I do here 100mm of extra ground clearance, which is a big help considering that the Range Rover suffers from a long rear overhang. The combination of the 40mm lift King springs and the standard length Koni shocks work extremely well.  I think the slightly softer spring rate over the 50mm springs is an asset.  To date I have only ever bottomed out the suspension system two or three times, and that was always at a very high speed and my own silly fault.  The Koni shocks are superb, and if you can afford them, they can't really be beaten for performance.  Getting the shock absorber dampening correct is just as important as the right spring rate.

I have also fitted "polly air springs" to the back to help when carrying heavy loads, and I also run these pumped up to about 20psi when driving on road to help stiffen the rear springs and reduce the body roll.

Full view of the rear spring with packer and "Poly Air Spring" fitted.

 

So what does the future hold? 

On the drawing board are a set of extra long travel Old Man EMU shock absorbers.  These shock absorbers increase the overall axle articulation by 60-80mm depending on how they are mounted.

I intend to replace the existing rubber bushed rear swing arm assembly with a Hemi jointed design.  This will reduce the stresses on the arms and chassis at full cross up.

I have also fitted a set of Polly Air bags to the rear springs to allow me to change the spring rate when out camping and carrying an extra heavy load.

I am still not 100% happy with the on road handling and intend to have the swivel housings machined so that I can rotate them on the axle flanges and get the king pin angle exactly right.